Negative LTFT at Idle, KR at WOT

Discussion in 'Mazdaspeed 3 Troubleshooting' started by Duey1083, Jul 22, 2021.

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  1. Duey1083

    Duey1083 Greenie Member

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    Hey everyone,

    @Enki I'm creating this thread as per your suggestion.

    In March / April, I took it upon myself to walnut blast the intake valves, service / clean the fuel injectors, replaced the injector seals with Overspeeds, replaced the PCV valve in the OEM PCV plate, and installed the DM Stage 1 OCC. I also installed a 3 bar MAP sensor at this time and had the tune revised by Stratified to account for this change; I did this in anticipation of doing a BNR S3 install...not so sure about it anymore, lol.

    Mods on the car: JBR 3" aluminum tru-wide air intake, Test Pipe, 3" SU TMIC, 1-step colder plugs (NGKs) gapped to 0.028" (if I recall correctly...this was done a year ago), DM Stg 1 OCC (PCV -> OCC lower port, OCC top port -> long hose -> check valve into intake manifold), Accessport v3, Stratified Stg 2 91 octane tune.

    The car ran fine right after I put it all back together, but over the last couple of weeks I have noticed that the LTFTs have gone to -12.5% to -14.09% during idle. While it idles, I can hear the car constantly adjusting something (maybe the injectors or something)...idle is fairly stable, but AFR sometimes jumps around from high 13s to low 15s (this issue is only intermittent for some reason and wasn't caught in the datalogs). LTFTs are within normal range during partial throttle cruising.

    I decided to try a WOT pull in 3rd gear, but had to abort it twice before redline due to high KR (3.69 peak).

    I thought the issue might have been that the coupler for the intake to the turbo was loose, so I re-seated it, but the issue has returned. I was extremely careful putting the car back together, following the FSM torque specs and sequences for the fuel rail, intake manifold, and throttle body.

    Maybe unrelated, but worth mentioning:
    - When putting the car back together after cleaning the valves, I had stupidly used a bit of green scotchbrite to clean the intake manifold gasket surface on the engine block. I didn't go to town with it, but tried my best to clean the runners as thoroughly as possible after realizing my mistake. When I changed the oil last night, I am noticing a bit of metallic material in the bottom of the drain pan when draining it into a used oil container. I change oil on 3 cars, so I'm not sure which one it is from...but likely not the fiances Rav4.

    Thank you for reading, and thank you in advance for any help.

    Andrew
     

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  2. Enki

    Enki Motorhead Platinum Member

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    What I see:

    In the idle logs, everything looks fine, but the boost pressure seems off to me for some reason. What is the KOEO value for boost for you?
    The only other thing in the idle logs is that you're pulling a fat grip of fuel, which suggests to me you need a MAFCAL.

    For the WOT logs, it kinda looks like you either have bad plugs, bad fuel or something else that's causing the combustion event to go out of control; the persistent knock is causing it to richen up a ton, and even that isn't helping with the KR. The step colder plugs alone should be enough to pull out some pump gas KR.

    Try putting a gallon or two of E85 in the tank on your next fillup if you can (shouldn't need a retune for just this one tank) to see if it helps the issue at all. If it does, maybe you got shitty gas? As a side note there's a possibility it will be harder to start and run kinda shitty till it comes up to temp; this is because E85 doesn't like step colder plugs, but I wouldn't worry about that too much, since it's just a test and shouldn't really impact normal driving.
     
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  3. Duey1083

    Duey1083 Greenie Member

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    Thank you @Enki

    What does KOEO mean?

    I thought so too about the boost pressure at idle...should be more vacuum, right?

    I had the MAFCAL checked last year before the map revision to account for the 3 bar MAP sensor. The tuner said it was great at that time.

    I'll pull the plugs to do a compression test soon and will review them.

    As for the gas, I filled up at Shell, which should be good...I do have some e85 kicking around from last year that I could add to the tank.

    In Shoutbox you mentioned the purge valve as a possibility. How should I validate that?
     
    Duey1083, via a Samsung mobile device, Jul 22, 2021
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  4. Awafrican

    Awafrican Moderator Gold Member

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    Key on engine off = KOEO
     
    Awafrican, via a mobile device, Jul 22, 2021
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  5. Enki

    Enki Motorhead Platinum Member

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    KOEO Key On Engine Off. Should let the AP work properly even if the car isn't running; just need to know the boost number in this state, which should tell you if your calibration for the MAP sensor is on point or not. You could also get a decel log (engine braking) which should see really high vacuum numbers.

    For the purge valve you could disconnect and plug the hose or just clamp the hose and see if trims change.

    I'd be careful using old E85 as it tends to attract water. If it looks like it has separated out into different fluids or is cloudy, don't use it.
     
  6. Easter Bunny

    Easter Bunny Professional Engineer Motorhead Platinum Member

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    KOEO key on engine off

    Turn the car all the way on but don't start it
     
    Easter Bunny, via a mobile device, Jul 22, 2021
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  7. Duey1083

    Duey1083 Greenie Member

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    Okay, thanks guys...appreciate the help.

    I'll try that out and see what I get. I'll also try to give the MAF a clean.

    EDIT: KOEO boost levels are 0.15 psi...so seems to be okay.
     
    Last edited: Jul 22, 2021
    Duey1083, via a Samsung mobile device, Jul 22, 2021
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  8. Enki

    Enki Motorhead Platinum Member

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    Change your air filter as well, if you've not done that in a year or so.
     
  9. Duey1083

    Duey1083 Greenie Member

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    So quick update...there are no updates, yet.

    I was looking at the condition of some of my hoses and vaccum lines. I found that the valve cover breather to the intake was a bit loose and had partially slipped off.

    I also noticed a hairline crack in the BPV recirculation hose where it clamps to the BPV. I'll be ordering a replacement from JBR shortly...shipping is expensive to Canada, is there anything else I should purchase with my order while I'm going through all this? I was thinking of replacing the intercooler piping with the JBR stuff, but read mixed reviews.

    Next steps:

    1) Clean the MAF sensor
    2) Clean the air filter
    3) Perform compression test
    4) Add gallon of e85 and do another WOT datalog
    5) Replace BPV recirc hose

    If none of those indicate anything, I will send my logs over to Stratified for them to review if anything is amiss in the tune.
     
    Duey1083, via a Samsung mobile device, Jul 26, 2021
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  10. Awafrican

    Awafrican Moderator Gold Member

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    JBR hoses for tmic are good, no issues personally I wouldn't run them for Fmic but others do without issue
     
    Awafrican, via a mobile device, Jul 26, 2021
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  11. Duey1083

    Duey1083 Greenie Member

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    So I ordered JBR BPV recirc hose and intercooler hoses, as well as the JBR thermal insulating intake manifold and throttle body gaskets.

    I'm starting to suspect a leak from the throttle body...i had issues torquing the throttle body to the intake manifold.

    EDIT: what is the best way to clean the threads that are drilled into the block? If I pull the intake manifold off again, I would like the clean them out to remove any oily residue that may be throwing my torque readings off.
     
    Duey1083, via a Samsung mobile device, Jul 29, 2021
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  12. Awafrican

    Awafrican Moderator Gold Member

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    Hit it with some break cleaner then some compressed air will clean out the threads nicely
     
    Awafrican, via a mobile device, Jul 29, 2021
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  13. Cfoldone

    Cfoldone Gold Member

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    Also run a tap to clean up threads too.
     
    Cfoldone, via a mobile device, Jul 29, 2021
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  14. Duey1083

    Duey1083 Greenie Member

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    So I ran a compression test on the engine and it all checks out okay:

    Comp 1: 169
    Comp 2: 170
    Comp 3: 172
    Comp 4: 167

    I've uploaded some pics of the spark plugs as well...they look a little sooty, but i also only took the car for a short drive around the neighborhood before doing the compression test.

    I'm cautiously optimistic, but my LTFTs at idle are around -5.47% to -6.25%; approximately 70 miles since I last reset the ECU.

    Troubleshooting done to date:

    Cleaned MAF and air filter
    Foil taped the BPV recirc hose (waiting for new JBR to replace it)
    Re-secured the valve cover breather line to the intake (found it loose)
    Re-secured the coupler from the intake to the turbo inlet
    Checked and re-gapped plugs to 0.028"

    As mentioned, trims appear to be improved; however, it may still be too early to tell. I'll keep driving it around casually for a few more miles. I'll then try another WOT run once I have the new recirc hose installed.

    OIL Concerns:

    I mentioned I noticed a bit of metallic flake on the bottom of the drain pan I use. I cut open the filter using tin snips and found a few flakes in the fins of the filter media. Not sure if these are magnetic or not as they are quite small and embedded into the media.
    20210730_122908.jpg 20210730_122921.jpg 20210730_122932.jpg 20210730_122945.jpg
     
    Duey1083, via a Samsung mobile device, Jul 30, 2021
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  15. Duey1083

    Duey1083 Greenie Member

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    So I rechecked the PCV and OCC setup. The PCV retainer ring was secure, all hose clamps were tight and secure also. The check valve arrows point towards the intake manifold.

    While I have the car on jack stands, I was thinking I could snoop check the test pipe I installed last year to check for leaks.

    @Enki, should I just be disconnecting the line from the purge valve and then plugging it with my hand to see what it does to my trims? Or does it need to be disconnected while driving around a bit to diagnose it?

    I'm starting to run out of things to check now, without removing and reinstalling the intake manifold and throttle body. Oddly enough, my LTFTs started to dip again to -10.16% yesterday and when I left the car idling, they started improving again to -7.03%. It has been about 120 miles since the ECU was last reset, so maybe it's still relearning?
     
    Duey1083, via a Samsung mobile device, Aug 1, 2021
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  16. Enki

    Enki Motorhead Platinum Member

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    Yeah you can thumb it at idle to see if the engine changes sounds with it on vs off. You could also just pinch the line.

    Also you can't really trust idle trims since so many variables can change trims and at idle it's basically magnified 100x.
     
  17. Duey1083

    Duey1083 Greenie Member

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    I removed the hose and put my thumb on the end and no difference between it connected to the purge valve or being plugged by hand.

    So I think the purge valve is good.

    I think I will just drive it around like normal for now and install the JBR BPV recirc hose when I get it, and try a WOT pull then.

    Other than that, I'll reach out to Stratified to see of they can find anything wrong.

    I don't want to invest too much money in the event the engine is actually going bad. Anyone know off-hand the number of hours a shop would charge to remove and reinstall a long block? I will call a couple shops in town.

    I'm thinking this is outside of skills and time allotment, and just trying to decide what to do for a worst case scenario.
     
    Duey1083, via a Samsung mobile device, Aug 2, 2021
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  18. Duey1083

    Duey1083 Greenie Member

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    @Enki / @Awafrican, I was doing some reading on the forums, and I was wondering if I should also explore the pressure relief and spill valves as a potential culprit? I also read that seals within the HPFP could be a cause of rich LTFT at idle issues...and as noted by @Enki, my car is running pig rich during WOT runs as well.

    What function does the spill valve on the HPFP perform? I'll read the thread regarding the HPFP tear down, clean and rebuild.

    At this point, I don't think this is a vacuum leak. I also don't believe this is a MAF sensor issue as there is no obvious behaviour and I checked to ensure the calibration was the same by comparing it to last year's WOT runs. The voltages and g/s correlate with last year's run.
     
    Duey1083, via a Samsung mobile device, Aug 2, 2021
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  19. Enki

    Enki Motorhead Platinum Member

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    You'd be fine with stock seals; it's what I use and no issues there. The only way seals can cause an issue is if they leak enough to flood your oil with fuel, in which case, you have vastly more serious issues than running rich at idle.
     
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  20. Duey1083

    Duey1083 Greenie Member

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    As a bit of an aside to my thread, @Awafrican, part of my recent mods was to relocate the ECU to the top of the fuse box as I found it had been rubbing on the intake.

    I'm having some issues with the relocation due to the cables, which are bound by the white plastic protector.

    Am I okay to remove that shield? Pretty nervous about damaging the wiring harness and wasn't sure if that is required. It is putting strain on the positive battery cable though.

    EDIT: uploaded picture.
     

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    Last edited: Aug 6, 2021
    Duey1083, via a Samsung mobile device, Aug 6, 2021
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