Heavy misfire under load

Discussion in 'Mazdaspeed 3 Troubleshooting' started by Gabriel Buscema, Aug 26, 2024.

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  1. Gabriel Buscema

    Gabriel Buscema Greenie N00B Member

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    Hey guys! I need some help. My car stutters/chops/misfire under load.

    Here is some information about my car:
    2007 mazdaspeed3
    Engine was rebuilt 3 months ago (bent rod lmao)
    FBO, BNRs4, middle of getting tuned with Justin using versatuner

    Here's a further explanation of my issue:
    When slowly increasing rpm of the car (like 10 percent throttle) the car acts and drives fine and idles like normal
    When you give it any more than 10 percent or any load, it suddenly starts "chopping" and misfiring
    Will throw an occasional p0300 code but it's rare and when I'm REALLY fucking with it

    Now here's what I've tried already
    Replaced plugs
    Rotated a new coil through all 4 cylinders
    Swap in 4 used coils
    Compression test (170 on all 4)
    Checked grounds
    Added an extra ground wire from the hpfp to the chassis
    Verified spark in all 4 using a coil pack tester
    Verified fuel pressure is good
    Verified prv is working
    Cleaned MAF
    Swapped back in stock map sensor
    Verified it is in time
    Replaced crank sensor and cam sensor
    Took an oscilloscope to the injector plugs (as per Justin's recommendation) and verified a pulse to all 4 injectors from the ECU
    There might be more that I cant remember right now
    This is my daily so the sooner I can get it running the better
    Thanks!
     
    Gabriel Buscema, via a mobile device, Aug 26, 2024
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  2. Raider

    Raider Administraider Administrator Platinum Member

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    @Gabriel Buscema Just saw this. If you sourced the plugs on Amazon, that could be why. They are fakes. Also check plug gap. .026 is ideal. Oem coilpacks only.
     
    Raider, via an iPhone, Aug 31, 2024
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  3. Easter Bunny

    Easter Bunny Professional Engineer Motorhead Platinum Member

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    It almost sounds like it's getting too much fuel. Like if you try to floor a car with a carburetor before it's warmed up

    What size intake do you have?
     
    Easter Bunny, via a mobile device, Aug 31, 2024
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  4. Gabriel Buscema

    Gabriel Buscema Greenie N00B Member

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    It was off a part out car, so they are confirmed OEM. And like I (might) have mentioned I rotated through a brand new single one as well
    Plugs were from the local O'Reilly's
     
    Gabriel Buscema, via a mobile device, Aug 31, 2024
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  5. Gabriel Buscema

    Gabriel Buscema Greenie N00B Member

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    3.5 inch damond motorsport intake, the MAF is calibrated and was working before this issue suddenly popped up
    Also I'm getting no rich or lean codes, just the random misfire only on startup
    Also threw a smoke machine on the intake and there are 0 boost leaks
    AFRs looked fine too I think? Idk id have to check back through the log lol
     
    Last edited: Aug 31, 2024
    Gabriel Buscema, via a mobile device, Aug 31, 2024
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  6. Raider

    Raider Administraider Administrator Platinum Member

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    What has Justin said about the logs of this? Probably good to upload here.
     
    Raider, via an iPhone, Aug 31, 2024
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  7. Cfoldone

    Cfoldone Gold Member

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    While mine was being tuned by damond also with VersaTune. Found that at the upper end of fueling flows for IDC max that my old Hpfp internals would fail to have maximum sustained pressure. So I needed to halt tuning. I replaced HPFP internals and a full teardown cleaning of PRV. IDC % would climb but was leaning out from logs. That was the cure.
    Please post logs, especially ones that you send to Damond for fine tuning of your specific tuning needs.
     
    Cfoldone, via a mobile device, Sep 1, 2024
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  8. Gabriel Buscema

    Gabriel Buscema Greenie N00B Member

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    Besides testing the ECU with an oscilloscope, Justin hasn't said too much. Here are the logs that I sent Justin
    Recently I pulled injectors and I found that
    1. They were all super dirty
    2. previous owner only put aftermarket seals on 3 of the injectors?? not 4??
    Justin basically said one of my seals was defiantly blown and could be the cause of misfiring
    The injectors are currently on their way to SP63 for their cleaning and flow testing, and will also redo all the seals as well
    IMG_20240829_170621892.jpg 5b22db79-4da0-4c99-9173-255cdf109aeb.jpg
     

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  9. SyntheticAtmosphere

    SyntheticAtmosphere You only get ONE ride, ONE ticket, ONE time! Silver Member

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    Theres your sign...Hope it gets you back up!
     
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