P0300 - Rough cold start

Discussion in 'Mazdaspeed 3 Troubleshooting' started by BoostFever, Oct 16, 2024.

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  1. BoostFever

    BoostFever Silver Member

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    Year/Make/Model: 2011/Mazda/Mazdaspeed3
    Mileage: 105k
    Location:
    Washington, US
    Concern: Rough cold start and P0300
    DTC's: (please include descriptions): P0300
    Modifications: Stock
    ECU/Tuning Software: None
    Tuner: None
    Is the concern intermittent? No
    Can you duplicate the concern?
    Yes
    Recent Repairs:
    N/A
    Correction: N/A

    Hey guys, I've a 2011 Gen2 Speed 3 with 105k miles. I spun a bearing last year, due to low oil, and had my engine replaced. A very painful lesson very well learned. I supposedly got a "Grade A" engine with <45k miles.

    Since it has been replaced I've had a P0300 error on cold starts but only when it's warmer than 19C / 68F. The start up is very choppy and cuts in and out until everything is fine and smooth. I've taken the car to AutoX and also a track day with a handful of 20 minute sessions at both. Engine ran perfectly fine.

    So far I've replaced the coils with OEM coils and replaced the spark plugs with pre-gapped NGK plugs. But no luck.

    I've scavenged old threads and have come up with the follow things to do next:
    • Check cylinder compression
    • Clean MAF sensor
    • Check for vacuum leaks (smoke test)
    • Check / clean injectors (most expensive option for last)
    I've attached a FORScan datalog during cold start, I can easily add more PIDs and re-run if helpful.

    What else should I be doing? Is there something super obvious in that datalog?

    Any help is really appreciated, I just want my old reliable speed 3 back.
     

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    Last edited: Oct 16, 2024
  2. Raider

    Raider Administraider Administrator Platinum Member

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    It's a JDM motor, isn't it? Those are 99.69% junk.

    Compression test is needed. Then leak down. Also if using aftermarket coilpacks, those suck too. Pics of motor?
     
    Raider, via an iPhone, Oct 16, 2024
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  3. BoostFever

    BoostFever Silver Member

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    I'm not sure where they got the motor honestly. I swapped out the coil packs with an OEM set and that didn't solve it.

    I've a compression tool coming in the next couple of days. Will post results and photos of the motor.
     
    BoostFever, via a mobile device, Oct 16, 2024
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  4. Raider

    Raider Administraider Administrator Platinum Member

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    Also check the plug gap. .026-.028. Sometimes the pregapped ones are not right.
     
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  5. BoostFever

    BoostFever Silver Member

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    I rechecked the pre-gapped plugs, all at 0.028.

    Did the compression test, motor warm. I ran the tests four times per cylinder, changing cylinder after each single test.

    I realized I didn't have the throttle fully open for these, but it does look like cylinder #1 is the outlier. Should I be concerned with that difference?

    • Cylinder 1
      • Test#1 - 180
      • Test#2 - 180
      • Test#3 - 185
      • Test#4 - 185
    • Cylinder 2
      • Test#1 - 190
      • Test#2 - 190
      • Test#3 - 200
      • Test#4 - 200
    • Cylinder 3
      • Test#1 - 190
      • Test#2 - 190
      • Test#3 - 195
      • Test#4 - 195
    • Cylinder 4
      • Test#1 - 180
      • Test#2 - 190
      • Test#3 - 195
      • Test#4 - 195
    Motor photos attached.
     

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    Last edited: Oct 17, 2024
  6. Raider

    Raider Administraider Administrator Platinum Member

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    Next step would be to get injectors pulled. Look for leaks. Then get em tested and cleaned and good seals like CorkSport, and new o rings.
     
    Raider, via an iPhone, Oct 18, 2024
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  7. BoostFever

    BoostFever Silver Member

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    I guess a leaking injector lines up with the constant long-term negative fuel trip in the datalog?

    Thanks for this. I have the CS fuel injector removal tool coming. I'll take them out and get them cleaned. Seems SP63 is where everyone recommends?
     
  8. BoostFever

    BoostFever Silver Member

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    Pulled those suckers out. Looks like they're pretty grimy. Sending them off to get cleaned. Not seeing any leaks around the injectors, though injector #2 came out in my hand without any effort oddly.

    Valve carbon buildup seems pretty bad on some. I might try to clean those while I have it all apart.

    Also going to replace PCV valve while I'm here.
     

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