Wastegate Duty Cycle Way Too High - Need a Wizard

Discussion in 'Mazdaspeed 6 Troubleshooting' started by oranjes, May 22, 2022.

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  1. oranjes

    oranjes Greenie Member

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    Been tuning with Justin @ Freektune and he has recently given up in ideas on what's screwing with my boost pressure. He's had me change my wastegate spring from 17 PSI up to 21PSI but no dice. Other brains trusts I have consulted are also short on answers.

    Engine mods are:
    Damond PCV Plate
    CS Intake & Exhaust Mani
    CST5 IWG
    Port Injection
    100 cel cat
    HDIGT2 w/ Mishimoto G-Line core
    GFB BOV
    3.5in HTP intake
    on 98 octane (australian, think its 93 US)

    As for most pertinent to possible intake issues, I have a bespoke catch can setup (in Damond's "bye bye blow-by" blog it's the last one they discuss), as well as a Cobb 3 Port EBCS and a Guardian Angel V3 and am using the GA's MAP sensor. All these have been tested, no leaks and all clean. May need to swap out my EBCS - could've gone bad, but doubtful. Everything I've changed between the WGDC being fine and it being a problem amounts to adding an airbox (which I removed just to simplify my issue hunting) and a boost, oil temp and oil pressure gauge (also removed boost gauge to simplify issues). I've had a couple tune revisions as well but I'm trusting that Justin knows what he's doing :p

    The typical behaviour is that it hits 75% WGDC as soon as I WOT and creeps up to 95% by 5500RPM.

    Please see attached logs. Log 91 is the last log before it started going haywire. Log 92 is when the issue really showed itself. Log 111 is where I am currently at. Changes between then and now are a smaller intercooler core, a boost leak fixed, and the wastegate spring being put up to 21PSI. The only other thing I can think of is when my car shorted out for a moment (uncertain if this was between log 91 and 92), in which I could hear my EBCS solenoid flicking on and off very rapidly. Electrical gremlins?

    Cheers!
     

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    Last edited: Apr 7, 2023
  2. oranjes

    oranjes Greenie Member

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    for posterity the issue was my wastegate actuator was NOT tight enough

    now i am having a seperate issue that is robbing the car for 30-50kw, aiming at 260 - 280 or so with CST5 at 26psi (no port injection yet) and only reaching 230-250. compression test is alright. boost leak test next. any other ideas let me know
     
  3. Awafrican

    Awafrican Moderator Gold Member

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    Boost leak test for sure, which ebcs are you running? Corksports has been known to fail

    280kw (375hp) at the wheels would be about the max for stock fueling on the ms3, now 230-250kw (308-335hp) does seem a little low.

    That being said fresh plugs gapped to whatever freektune has advised (my guess is 0.026-.028"), clean MAF sensor.

    @Easter Bunny @Enki thoughts? you two know more about fueling limits than I do
     
    Awafrican, via a mobile device, Apr 7, 2023
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  4. Easter Bunny

    Easter Bunny Professional Engineer Motorhead Platinum Member

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    Boost leak test

    What is the condition etc of the high flow cat? Possible it is breaking up and blocking exhaust flow
     
    Easter Bunny, via a mobile device, Apr 7, 2023
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  5. oranjes

    oranjes Greenie Member

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    Swapped out the EBCS already from Cobb to CS as I was suspecting it for the wastegate issue previously. No difference at all between them

    The plugs are fresh and gapped 500km ago, had them out for a compression test and still looked good. Compression was good across all 4 with one inconsistency, in that a wet test didn't increase compression in cylinder 4

    Boost leak test didn't bring any enlightenment except telling me BOVs are always leaking a little but I will test again to make sure. Also tested the exhaust, and fairly satisfied it has no leak

    If you think a blocked high flow cat has a good chance of dropping me that much power I'll definitely check it out

    Will also clean the MAF
     
    oranjes, via a mobile device, Apr 23, 2023
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  6. Easter Bunny

    Easter Bunny Professional Engineer Motorhead Platinum Member

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    Have you cleaned the air filter?
     
    Easter Bunny, via a mobile device, Apr 23, 2023
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  7. oranjes

    oranjes Greenie Member

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    Should be fine, my car has had it for 500km and before that it was on another car for maybe a thousand. Will clean it anyhow
     
    oranjes, via a mobile device, Apr 23, 2023
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  8. oranjes

    oranjes Greenie Member

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    Just recording - air filter couldnt be much cleaner, still looks brand new
     
    oranjes, via a mobile device, Apr 24, 2023
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  9. oranjes

    oranjes Greenie Member

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    mine is a MS6 just FYI

    MAF sensor is cleaned

    boost was tested twice and all good there

    going to check the cat out soon
     
    oranjes, via a mobile device, Apr 25, 2023
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  10. oranjes

    oranjes Greenie Member

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    Cat looks good but there was a nut in it and the o2 sensor was sooty as hell. Will do a log and see if thats any difference.
     

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    oranjes, via a mobile device, Apr 28, 2023
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  11. oranjes

    oranjes Greenie Member

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    POWER

    Year/Make/Model:
    2006 Mazda 6 MPS/MazdaSpeed6
    Mileage (km): 204,000 on car, 18,000 on built engine. 500 since engine install
    Location: Australia
    Concern: Missing between 30 to 50kw worth of power compared to very similar cars. Making 230-250 (depending on Vdyno setup) when I am told 260 to 280 or even 300 should be possible. I am wanting to sort this before moving into port injection.
    DTC's: only on EGR and intake manifold flaps, for very normal and legal reasons

    Modifications:

    Built engine (forged rods and pistons, completely refurbished at time of building)
    Xtreme twin plate 1200nm clutch
    Damond PCV Plate and PCV setup according to most complicated setup in Damond's PCV blog
    CS Intake & Exhaust Manifolds
    CST5 IWG
    CS FMIC
    CS BOV
    CS turbo and manifold blankets
    Returnless port injection (not yet active but fuel to the HPFP is being ran through the port rail)
    Split Second Controller
    Guardian Angel V3 (using V3 for MAP sensor as well, spliced in with CS 3.5bar that came with the CST5)
    100 cel catalytic converter
    3.5in HTP intake
    less relevant ones are suspension such as all 3 Damond engine mounts, rear diff mount, coilovers, big brakes, transfer case caps, rear sway bar
    on 98 octane (Australian, which I think is 93 US)

    ECU/Tuning Software:
    Cobb AP V3
    Tuner:
    Freektune, AtenzaTuning
    Is the concern intermittent?: Constant
    Can you duplicate the concern?: Every datalog
    Recent Repairs: wastegate arm was not tight enough so this was corrected
    Attempted fixes thus far: ensuring crank position sensor is aligned, cleaning MAF, boost leak test, checked catalytic converter, checked compression
    Correction: None yet

    Thought I would post up in the proper format for posterity and keep it updated. Also see logs. Some are 3rd, some are 4th, some are idle.



     

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    Last edited: Apr 29, 2023
  12. Awafrican

    Awafrican Moderator Gold Member

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    Threads merged, creating multiple about the same issue is not helpful.


    Have you spoken to freektune about the issue? Might be the CS map sensor failing...wouldn't be the first. It could just be that you're engine doesn't want to do more....also you found a nut in your cat what?!
     
    Awafrican, via a mobile device, Apr 29, 2023
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  13. oranjes

    oranjes Greenie Member

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    Sorry, it's a different issue really which is why I did it, under a different title for more specific searches.

    And yea the CS 3.5 did fail, which is why I'm using the GA V3 built in MAP wired to the harness which is otherwise connected to the CS. But I am worried - if the CS main signal failed, could it be sending other things wrong as well other than the wire that I spliced into? What are each of the wires to the MAP for?

    As for the bolt yea, no idea Cant tell what its from, looks a little like an exhaust manifold locknut or even driveshaft maybe. Dont think it went through the engine.

    Also have not spoken to Freek since fixing my wastegate. Don't want to waste any more of his time until everything is sorted - he was at his wits end trying to sort that out.
     
    oranjes, via a mobile device, Apr 29, 2023
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  14. Awafrican

    Awafrican Moderator Gold Member

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    If your waste gate wasn't functioning that could be need a retune. Personally I'd swap that CS sensor for a Bosch one, I don't know the pin out on the sensor wires but yes if it's reading incorrect that'll send wrong to the guardian angle.
    Are you still running a CS ebcs as well, it's fully functional? Those fail too, one guy went through 3 of them here before swapping to a different one and issue resolved.
    You can make your own one pretty cheap
    https://mazdaspeeds.org/index.php?threads/how-to-diy-an-ebcs.10919/
     
    Awafrican, via a mobile device, Apr 29, 2023
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  15. oranjes

    oranjes Greenie Member

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    CS EBCS is functioning same as the one I pulled out to ensure the wastegate issue wasnt being caused by it, so fairly certain it's fine.

    As for MAP sensors maybe I'll chuck the OEM in just to be sure. Think the GA interprets and sends everything based on the pressure going through it rather than anything on the stock location MAP, but there are like 3 more wires to the stock location MAP so I dont know.

    Also want to clarify, I am hitting boost targets perfectly as far as I can tell. Look at the logs, near instant 20psi spool. Just low on power. It has been retuned since the wastegate issue too.
     
    oranjes, via a mobile device, Apr 29, 2023
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